I was the software guy on a product that used these type of connectors. The tiny "signal" pins worked fine. The big "power" pins - about 3 or
4 mm diameter - also worked fine, for at least a couple of hundred watts (48 V at a few amps).The co-ax connectors - the SMB-ish ones that fit in the same space as a "power" pin - didn't work at all. Or at least, the ones on the backplane didn't work.
For whatever reason, the co-ax inserts in the backplane connector didn't have solder pins sticking out the bottom, like the adjacent "signal" pins. Instead, they drilled a clearance hole in the PCB behind the connector body, and used a co-ax insert that clipped into the connector body and stuck through the PCB. The co-ax connector was attached to a small piece of hardline that took the signal elsewhere. In other words, when the connector body was first stuffed to the PCB, you had a bunch of signal pins that were soldered down to the back plane, and an empty hole where the co-ax would later go. Somebody clipped the hardline + co-ax connector into the connector body as a separate assembly step.
In practice, when you slid the card (with mating co-ax connector) into place, it didn't always land square on the co-ax connector in the backplane. There were ramps molded into the connector body, in an attempt to guide the card connector into the backplane connector, but they weren't always effective. The usual failure was that you would push the connector+hardline out of the back of the connector body on the backplane, and get no connection. If you really vigorously slammed the card home, you'd also mangle the co-ax connector on the card.
In production, the techs would leave the back panel open while they seated the card with that connector. Seating it was a matter of wiggling the hardline (in the back) and gently trying to seat the card (in the front) until the connectors aligned and it would seat fully. IIRC, eventually the field guys were trained how to reseat the connector+hardline in an installed unit.
Matt Roberds