Ok, so, to bring this thread up once again, I'm having a new problem :(
Once I realized that my feedback was connected to the switched output instead of the filtered output, I cut the trace and ran the wire to the output instead. I tried the circuit and it worked perfectly. Under load, the voltage did not drop like a rock, it stayed very steady, just like I wanted.
Well, I modified every other board I had with this simple modification, and low and behold, none of them work properly! Their voltages drop very very quickly under load. By approximately 1 amp average DC load, the output voltage has dropped 3 volts or so! The feedback is connected to the output, as it should be, and this still happens.
The data sheet indicates that the feedback voltage likes to sit at
1.21V. When checking the feedback voltage at the pin, it is indeed
1.21V. Under load, it drops according to the load. By 1A or so it is
800mV or less. I tried to check the duty cycle of the switching output to see if it increases as the feedback voltage decreases, which it should, right? I cannot get a good look at the duty cycle on my scope here. It is just sooo noisy, I can't really tell much of anything from it. From the way the output voltage dives so quickly, I can't imagine that the chip is paying any attention to the feedback voltage, but why?
An interesting thing that I tried, was to remove the inductor (15uH) and try different combinations of these inductors in series and parallel. Even though the inductor is far away from the feedback and any other wires I thought it would affect, the gator clips I used to connect the inductor(s) allowed me to move the inductor(s) far away from the circuit to ensure that it's EMI was not messing with anything. The combinations of inductance values here did not seem to make any difference, the output voltage was pretty smooth all the time, but the voltage drop was not effected by any different values.
Just to try it, I removed the inductor(s) entirely and shorted where the inductor connects with an alligator clip. Surprisingly (to me) it worked great. The output was a *little* noiser than with the inductor, BUT, there was almost no voltage drop (500mV at 2.1A load). Overall, an acceptable result. Funny enough, though, if I just used two pieces of wire (18 gauge I believe), and twisted them together, no luck, it did not work at all, very noisy output and it voltage dropped just like with the inductor. What gives with this?! What are the properties of your typical alligator clip connector (I confirmed this with a few different alligator clip connectors, all about 1 foot in length) that would cause this and make them so much different than a typical wire? Increased resistance? But is it really that much?!
So, to summarize, for some reason, the LM2678 seems to be ignoring it's feedback voltage level and does not seem to be increasing the duty cycle as the load increases. I should also note, that, on the same circuit board, I have a 9V regulator. It is the exact same chip and designed the exact same way (selecting recommended components per the data sheet) and it works GREAT. It is designed for ~3A load instead of
5A like the 6V, and therefore uses a different schottky, different inductor, and less capacitance, but it does not have voltage drop problems, it works great.
Any ideas? I'm very stumped. I'm going to spend a little more time trying to determine the duty cycle and see if it is in fact increasing as the load increases, but I suspect it is not, or I would not be having the problem I am having... right?